Servo Motor Shaft Modification
Posted by
cnc_4_me
on 2005-04-29 00:32:07 UTC
--- In CAD_CAM_EDM_DRO@yahoogroups.com, "John Stevenson" <john@s...>
John Stevenson said "Conversion was very easy".
John. What in the world would have been a difficult conversion? I
have read this post from you about 10 times in the last couple of
days. It sounds like you did everything but rewind the motor. And
how in the world did you do it? When I think about the practical
problems involved, it seems to me to be one of those things that
can't be done! You must be a super genius with a team of master
machinists helping you (well ok I am being a little facetious) but
holy cow.
1 When welding up the shaft it must have been glowing red. How did
you keep the wiring on the armature from burning up.
2 After welding and adding 1/2 inch shaft length you would not have
been able to turn the shaft back down by mounting it between
centers. How did you get the shafts to turn true.
3 What sort of welding did you use.
4 Did you make the brush holder adjustable for optimal running in
forward and reverse?
Wally
--- In CAD_CAM_EDM_DRO@yahoogroups.com, "John Stevenson" <john@s...>
>up with weld then machined this back
> Conversion was very easy.
> I stripped it down, removed the front bearing and built the shaft
> down to 16mm to suit the pulley that's going on it.took the oppertunity to extend the
> Bearings are 17mm so anything under that isn't a problem. I also
> shaft by weld by 1/2" or so.new 5/8" thick alloy plate up to
> I scrapped the original pressed steel front mounting and turned a
> carry the bearing, two thru bolts and 4 tapped holes to match upwith the bridgy.
John Stevenson said "Conversion was very easy".
John. What in the world would have been a difficult conversion? I
have read this post from you about 10 times in the last couple of
days. It sounds like you did everything but rewind the motor. And
how in the world did you do it? When I think about the practical
problems involved, it seems to me to be one of those things that
can't be done! You must be a super genius with a team of master
machinists helping you (well ok I am being a little facetious) but
holy cow.
1 When welding up the shaft it must have been glowing red. How did
you keep the wiring on the armature from burning up.
2 After welding and adding 1/2 inch shaft length you would not have
been able to turn the shaft back down by mounting it between
centers. How did you get the shafts to turn true.
3 What sort of welding did you use.
4 Did you make the brush holder adjustable for optimal running in
forward and reverse?
Wally
--- In CAD_CAM_EDM_DRO@yahoogroups.com, "John Stevenson" <john@s...>
>but I can only find two at 110volt.
> I have obtained two new units here in the UK same as the 10-1783
> problem is we don't have 110 volt here.one of these.
> I can get a couple of 240 volts ones and it would be worth trying
>up with weld then machined this back
> Conversion was very easy.
> First the bracket was cut and ground off.
> I stripped it down, removed the front bearing and built the shaft
> down to 16mm to suit the pulley that's going on it.took the oppertunity to extend the
> Bearings are 17mm so anything under that isn't a problem. I also
> shaft by weld by 1/2" or so.new 5/8" thick alloy plate up to
> I scrapped the original pressed steel front mounting and turned a
> carry the bearing, two thru bolts and 4 tapped holes to match upwith the bridgy.
>to centralise the mounting plate.
> I used a 500 count 'D' shaper HP encoder on the rear.
> I faced the rear housing yo to get a flat surface and made a bush
> The mounting plate has two mounting patterens, a two opposed holepattern and a 120 degree pattern.
> I used the 120 degree pattern as the 2 hole one overlaps thebearing hole.
> I drilled and tapped three 2mm screw holes and fitted the back.1/4" cut off the length of the short extension.
> The armature was supported in a steady on the rear bearing and a
> The rest was turned down to 1/4" diameter for the encoder to clampto.
> The motor was reassembed, the encoder cliped on and secured and itwas then reay to run.
> It works very well, very little cogging but at the moment it'slimited to a 24v power supply
>
Discussion Thread
cnc_4_me
2005-04-29 00:32:07 UTC
Servo Motor Shaft Modification
turbulatordude
2005-04-29 06:10:17 UTC
Re: (EASY????) Servo Motor Shaft Modification
R Rogers
2005-04-29 07:14:13 UTC
Re: [CAD_CAM_EDM_DRO] Re: (EASY????) Servo Motor Shaft Modification
R Rogers
2005-04-29 16:53:16 UTC
Re: [CAD_CAM_EDM_DRO] Re: Servo Motor Shaft Modification
Gregg Swanson
2005-04-29 19:00:21 UTC
RE: [CAD_CAM_EDM_DRO] Re: Servo Motor Shaft Modification
Polaraligned
2005-04-30 05:40:55 UTC
Re: Servo Motor Shaft Modification
Robert Campbell
2005-04-30 17:56:17 UTC
Re: [CAD_CAM_EDM_DRO] Re: Re: Servo Motor Shaft Modification
Bruce Pigeon
2005-05-01 14:20:28 UTC
Re: [CAD_CAM_EDM_DRO] Re: Servo Motor Shaft Modification